On the twelfth of June 2025, a Boeing 787-8, registered in India as VT-ANB, was working as flight Air India 171 for a passenger flight from Ahmedabad to London Gatwick. The Boeing Dreamliner crashed shortly after take off, killing all the crew, 229 passengers and 19 individuals on the bottom. One passenger survived with severe accidents. An additional 67 on the bottom suffered severe accidents.
The day after, I wrote in regards to the fundamental particulars and highlighted two credible theories for what had occurred: both the plane was badly misconfigured or that each engines failed. On the time, essentially the most compelling cause I might suppose for each engines failing was contaminated gas, though it appeared unlikely as that ought to have affected all plane refuelling on the airport that day. I concluded that there might be an extra “one thing else” that we had been lacking as a result of the main points thus far didn’t make sense.
That sadly has confirmed to be the case and it doesn’t look good. I’m going to deal with precisely the sequence of occasions as said within the preliminary report.

The plane arrived from Delhi flown below totally different crew. There have been no identified defects with the plane and the load and steadiness had been inside regular working limits.
The captain held an ATPL with over 15,000 hours expertise throughout a spread of plane, with 8,600 on kind. The primary officer held a CPL with 3,400 hours of which 1,128 had been on kind. Neither had flown over the previous 24 hours. They’d arrived at Ahmedabad the day gone by with a purpose to function flight Air India 171 that day. Each had enough relaxation durations. Each pilots handed their preflight Breath Analyser take a look at, which is normal process for all flight crew at Air India.
The primary officer was the Pilot Flying with the captain as Pilot Monitoring.
At 07:43 UTC (12:43 native time) the flight crew contacted ATC for pushback, which was authorised, adopted by the plane beginning up. ATC requested if the plane required the complete size of the runway and the crew confirmed that they did. At 08:07:33, the plane was cleared for take-off.
The plane accelerated alongside the runway and reached V1, the take-off determination pace, of 155 knots usually. The plane lifted off at 08:08:39 UTC. Within the air, the plane reached 180 knots indicated airspeed at 08:08:42, at which level the gas cutoff switches transitioned from the RUN place to the CUTOFF place.
The report makes use of the phrase transition, as a result of the flight knowledge solely tells us that the place modified. Nevertheless, a crucial piece of data is that there was a one second hole: one swap was set to CUTOFF after which, a second later, the opposite.
This video posted to Reddit exhibits the guards across the two gas reduce off switches in a Boeing Dreamliner. What one can see within the video, which is confirmed within the report, is that to vary the swap from the RUN place to CUTOFF place, you need to pull every swap out after which down. There are guards both aspect. The purpose is that it’s not attainable to by chance knock these switches out of place.
Gasoline reduce off switchbyu/emoemokade inaviation
So, each switches moved from RUN to CUTOFF, one after the opposite. Each engines started to lose energy because of the gas being reduce off, that’s, the report is obvious that this was a direct trigger and impact.
The phrasing of the dialog within the cockpit is essential; right here’s what the report says:
Within the cockpit voice recording, one of many pilots is heard asking the opposite why did he cutoff. The opposite pilot responded that he didn’t accomplish that.
The cockpit voice recording evaluation would come with which microphone picked up the voices: on the left or on the fitting. Thus, it’s completely identified which pilot spoke. The investigators made a transparent alternative to not launch the precise wording or to specify which pilot requested the query.
The report confirms that the Ram Air Turbine deployed through the preliminary climb, as many had noticed from the CCTV footage. This confirms that the engines misplaced energy, inflicting the RAT to deploy.

The plane started shedding altitude earlier than making it previous the airport perimeter wall.
At 08:08:52, the gas cutoff swap for the #1 engine transitioned from CUTOFF to RUN. The swap for the #2 engine transitioned to RUN just a few seconds later. This initiates a “rekindle and thrust restoration sequence”, that’s, the engines ought to routinely restart and start producing thrust once more.
In each instances, the engine relighting sequence began; nonetheless, it is a sluggish course of. The #1 engine was within the technique of spooling up. The #2 engine restarted however was not in a position to spool up and get better thrust. Successfully, each engines responded precisely as one would count on to having the gas reduce off and restored. The issue was that there wasn’t sufficient time for each engines to spool again up. Had the difficulty occurred just some minutes later, after the plane had gained altitude, the engines would have had sufficient time to restart and produce thrust.
One of many pilots declared an emergency at 08:09:05, calling MAYDAY MAYDAY MAYDAY.
The air site visitors controller requested for extra info however didn’t obtain a response.
The Flight Knowledge Recorder stopped recording knowledge six seconds after the MAYDAY name, at 08:09:11.

The report paperwork the wreckage, largely confirming what we already knew. The Dreamliner crashed into a number of buildings and broke into items earlier than catching fireplace. The flap deal with was discovered “firmly seated within the 5-degree flap place, in line with a traditional takeoff flap setting.”
Each gas management switches had been within the RUN place. The engine thrust levers had been discovered set to close IDLE however in accordance with the flight knowledge recorder, each remained set to take-off thrust till the crash, so it’s doubtless that the levers shifted in impression.
Principally, the wreckage evaluation thus far underscores the truth that the crew tried to revive gas circulate to each engines earlier than shedding management of the quickly descending plane.
Based mostly on preliminary investigation of the wreckage, there was no fault with the plane. The report notes explicitly that there are not any beneficial actions associated to the Boeing 787-8 or the Normal Electrical engines.
The report additionally referenced Particular Airworthiness Data Bulletin NM-18-33, which has been the reason for a lot hypothesis. This 2018 bulletin was in response to a lot of Boeing plane which had been delivered from the manufacturing unit with defective gas switches that might be moved too simply. This was not thought-about to require an airworthiness directive requiring necessary inspections.

Air India didn’t examine the switches of their fleet and weren’t required to take action. Extra pertinently, nobody had reported any points with the gas switches on the accident plane after the throttle management module was changed in 2023.
The essential level right here is that there are not any reported situations the place the switches moved themselves. It’s attainable that this fault had been on the plane with out remark for 2 years. If this had been the case, it’s nonetheless clear that an individual moved these switches one after the opposite; nonetheless, it will add weight to the concept slicing off the gas was not deliberate.
The logistics of the cockpit imply that the Pilot Monitoring was higher positioned to maneuver the switches with out it being instantly seen. The Pilot Flying, targeted on the take-off, may not instantly discover the motion. The reverse, the place the Pilot Flying moved the switches, can be extra noticeable. Throughout take off, with one hand on the controls and the opposite on the throttle, any such motion can be instantly entice consideration, particularly because the Pilot Monitoring needs to be scanning the devices and never concentrating on any single spot.
The ten seconds between the switches being moved and the query being requested appears related. Assuming that the pilot asking the query was not the pilot who moved the switches, then it appears more likely to have been a response to the engines spooling down adopted by a look in direction of the switches to see that they had been inexplicably set to the CUT OFF place. However these at the moment are logical guesses; we don’t know who spoke, we don’t know what induced them to talk, and we don’t have any strategy to interpret the response.

The preliminary report makes it clear that the investigating workforce have further proof to overview, together with the postmortem experiences and statements from witnesses and the surviving passenger. Perhaps they’ll discover one thing that may shed extra mild on what occurred within the cockpit.
It might simply be inconceivable for the investigation to show who moved the switches, as they’re centrally situated in order that each pilots have entry. What we all know: somebody moved each gas switches to the cut-off place. We don’t know who did this. We have no idea if it was a deliberate motion or a deadly mistake. Extra importantly, it will not be attainable to ever know what the intent was.


