On Monday the sixteenth of June 2025, a twin-engine airplane crashed onto the roof of a hangar.

The plane was a 50-year-old Beechcraft King Air E-90, registered within the US as N1UC (serial quantity LW-140) with a legitimate airworthiness certificates till June 2031. On the time of the accident, the King Air had 10,922 complete airframe hours and 9,505 cycles. The pilot holds an Airline Transport Pilot certificates, the very best stage of pilot certification issued by the FAA, with an ATP ranking for Airplane Multi-engine Land such because the King Air. He holds kind rankings for a variety of advanced plane together with the Airbus A320, Boeing 727 and 747, the Beechjet 400, the Cessna Quotation 500 and others. Though his flight hours haven’t been launched, they possible exceed that of the King Air.
The flight departed usually from Missouri, the place the pilot is predicated, for a brief non-public flight to New Century AirCenter in Gardner, Kansas. (Fox Information reported that flight originated from Butler Municipal Airport, which brought on me a superb 20 minutes of confusion, as Butler Municipal Airport is in Georgia. The flight really departed from Butler Memorial Airport (KBUM), which is positioned in Missouri.)
There have been two on board: the pilot and one passenger. The climate in Kansas was heat with mild winds and damaged clouds at 3,400 toes. They have been within the last section of their flight, flying south on method to runway 18 at New Century AirCenter.
The information on ADS-B Change exhibits that the King Air had slowed to 140 knots for the method because it crossed the freeway. In line with early reviews, the left engine failed.
With the proper engine nonetheless producing energy, the King Air veered to the left, nonetheless descending. At about 13:15 native time, the airplane crash-landed onto the roof of the Butler Avionics hangar.

(Butler Avionics bears no connection to Butler Memorial Airport or Butler Municipal Airport, however modified its title from King Avionics to Butler Avionics after it was acquired by the Butler Nationwide Company in 2010. Butler Nationwide Company additionally has nothing to do with Butler Memorial Airport or Butler Municipal Airport however took the title in 1960 after the Nationwide Connector Company merged with an aviation analysis agency owned by the Butler household. Herewith endeth my temporary obsession with all of the Butler references on this case.)
The pilot is claimed to have then misplaced management of the plane but it surely certain appears like he managed to flare because the King Air clearly got here down on prime of the hangar roof versus crashing into it. It looks as if the plane will need to have spun nearly 180° as they impacted, possible the propeller of the working proper engine digging into the roof.
First responders rapidly arrived on the scene, together with the Johnson County Sheriff’s Workplace, Kansas Freeway Patrol, Hearth District #1, and MED-ACT.
The firefighters from Hearth District #1 arrange a ladder to achieve the roof and laid down foam suppressant as gasoline was leaking into the hangar under. The pilot and his passenger have been in a position to launch their security restraints and climb out of the plane, with firefighters rapidly concluding that they’d solely “non-life-threatening accidents”. Hearth crews helped the 2 down from the roof and transported them to a close-by hospital for remedy of minor accidents. Not one of the employees contained in the hangar was injured, though that will need to have been fairly a shock! The airport closed to site visitors for about an hour however there was little or no disruption to operations.
This 90-second clip displaying aerial footage of airport and the hangar was posted to a Russian-language aviation channel on Telegram.
2025.06.16. Emergency touchdown of Beechcraft E90 King Air N1UC on the roof of a hangar at New Century AirCenter (JCI/KIXD), Kansas state. The plane misplaced energy within the left engine and in consequence fell onto the hangar roof throughout method to runway 18. The pilot (73) and his passenger (30) obtained minor, non-life-threatening accidents. ABC Information by KMBC
This video isn’t from ABC Information, so I believe the credit score refers to the place the crash data was sourced, reasonably than the video itself. Nonetheless, I believe it may be the complete video from Information Chopper 9, based mostly on this excerpt posted on KMBC 9’s YouTube channel.
The hangar stood up comparatively nicely to being landed on with a King Air. Honestly, the King Air couldn’t have picked a greater place to land, as Butler Avionics specialize in King Air upkeep and restore.
Kansas Freeway Patrol filed a report {that a} car crashed right into a constructing (“Hit and Run: No”) 500 toes west of Previous U56. In line with the crash log, a mechanical malfunction brought on the left engine to turn out to be inoperable.
Thus far no CCTV or ATC recordings from the incident have been launched. A poster from the native space on the r/aviation subreddit stated that they have been cleared to land on Runway 18 however then referred to as for a go-around as a result of failure of the left engine.
One other poster tried to evaluate the injury:
Appears just like the left wing is a bit of wonky. The left engine is completely fubar. The correct engine appears equally fooked. The gear in all probability gained’t maintain the load anymore. Fuselage pores and skin wants exfoliation and a shit ton of moisturizer.
One other touch upon the topic was from an A&P mechanic
Truthfully, kudos to the blokes at Beechcraft. I might not have anticipated an aluminum airplane to seemingly win in a combat with a metal constructing, however that King Air appears prefer it could possibly be made airworthy once more.
Full credit score to the hangar as nicely, which stood agency, supporting the King Air 90 and defending these beneath.
There’s not but any data on what occurred to the left engine, considered one of two Pratt & Whitney Canada PT6A turboprop engines outfitted with Raisbeck four-bladed propellers. Juan Brown reviews that the left engine was not feathered, which needs to be an instinctive response within the occasion of an engine failure, though he additionally added that one blade “appears prefer it’s practically twisted into the feathered situation”.
Juan Brown believes {that a} key level for the investigation can be to determine whether or not this was an precise engine failure or a observe single-engine method. He says that the King Air was travelling at 86-87 knots earlier than crashing into the hangar whereas the minimal management velocity for the King Air with an engine inoperative (Vmc) is 86 knots, so it isn’t clear to me why the very skilled pilot misplaced management. Juan Brown additional reviews that the plane was travelling at 81 knots at time of impression, however this appears to be based mostly on ADS-B information which is notoriously unreliable at low stage.
Bryan Johnson, the manager director of the Johnson County Airport Fee, expressed reduction that nobody was severely injured.
Anytime the decision goes out {that a} airplane goes right into a hangar constructing, it stings a bit. However once more that’s why you’ve acquired professionals to handle the quick wants of these on the plane and ensure everybody’s secure on the bottom too.
The airport workers have reported that they’re collaborating with the NTSB and the FAA for a proper investigation into the reason for the crash.
Full credit score to @jpdemer5 who commented on Youtube with “King on a Sizzling Tin Roof” which I promptly stole to make use of because the title of this put up.


