India’s Plane Accident Investigation Bureau (AAIB) has launched its preliminary report on the Air India flight AI171 crash, pointing to a cockpit gasoline swap error and elevating questions on pilot actions.
The London-bound Boeing 787-8 Dreamliner skilled a deadly lack of thrust simply seconds into flight, with investigators now specializing in the sudden motion of cockpit gasoline switches and the next lack of engine energy.

Gasoline Cutoff Error Beneath Scrutiny
On the coronary heart of the investigation is a sudden transition of each engine gasoline management switches from “RUN” to “CUTOFF” shortly after takeoff. In keeping with flight recorder knowledge, this occurred because the plane reached its most recorded velocity of 180 knots at 08:08:42 UTC.
“The plane achieved the utmost recorded airspeed of 180 Knots IAS at about 08:08:42 UTC and instantly thereafter, the Engine 1 and Engine 2 gasoline cutoff switches transitioned from RUN to CUTOFF place one after one other with a time hole of 01 sec,” states the AAIB report.
This motion, usually reserved for floor procedures, abruptly shut down gasoline provide to each engines, inflicting them to lose thrust throughout a essential part of flight.
The cockpit voice recorder captured a short, startling trade between the 2 pilots.
“One of many pilots is heard asking the opposite why did he cutoff. The opposite pilot responded that he didn’t achieve this.”
Nonetheless, the report doesn’t make clear which pilot moved the switches or whether or not it was unintentional or unintentional. Through the takeoff, the co-pilot was flying the plane whereas the captain was within the monitoring function.

Failed Engine Restoration
Moments after the gasoline cutoff, the pilots reversed the swap positions, making an attempt to revive engine performance. The Boeing 787’s Full Authority Digital Engine Management (FADEC) system robotically started the ignition and gasoline introduction sequence.
“When gasoline management switches are moved from CUTOFF to RUN whereas the plane is inflight, every engine’s full authority twin engine management robotically manages a relight and thrust restoration sequence,” the report explains.
Nonetheless, solely one of many engines confirmed partial indicators of restoration.
“Engine 1’s core deceleration stopped, reversed and began to progress to restoration,” whereas “Engine 2 was in a position to relight however couldn’t arrest core velocity deceleration,” the report stated.
Regardless of these efforts, it was too late. The airplane had already begun to lose altitude, crossing the airport perimeter wall earlier than slamming into the close by BJ Medical Faculty and Hospital hostel advanced, killing dozens of individuals on the bottom.
Emergency Response and Closing Moments
Seconds after the gasoline switches had been toggled again to RUN, the cockpit recorder captured the ultimate misery name.
“MAYDAY MAYDAY MAYDAY,” one of many pilots shouted.
ATC tried to contact the plane’s callsign however acquired no response. The air visitors controller reportedly watched helplessly because the plane crashed within the distance.
Airport CCTV footage confirmed that the Ram Air Turbine (RAT), an emergency backup energy supply, was deployed throughout the plane’s transient preliminary climb. Nonetheless, this measure was not ample to stabilize or keep away from the crash.

Wreckage and Chicken Strike Concept Dismissed
Within the aftermath, AAIB investigators secured and examined the wreckage. Each engines had been retrieved and quarantined for additional evaluation. Elements deemed vital had been additionally remoted for detailed inspection.
“Wreckage website actions together with drone images and videography have been accomplished,” the report confirmed.
Crucially, the preliminary report addressed hypothesis {that a} chook strike might have brought about the crash. Nonetheless, surveillance footage and radar knowledge present no indicators of chook exercise alongside the flight path.
“No vital chook exercise is noticed within the neighborhood of the flight path,” the report famous.
This successfully guidelines out chook strike as a contributing issue.
Pilots’ Expertise and Background
The captain of flight AI171 was a 56-year-old veteran with greater than 15,000 flying hours, whereas the co-pilot was a 32-year-old with 3,400 hours. The First Officer was the pilot flying (PF) throughout takeoff, whereas the captain served in a supervisory capability.
The report doesn’t but draw conclusions about potential pilot error however highlights the deal with the sudden gasoline swap motion.

No Plane or Engine Fault Recognized
Considerably, the AAIB has discovered no quick technical fault with the Boeing 787-8 plane or its GE GEnx-1B engines.
“At this stage of investigation, there aren’t any advisable actions to B787-8 and/or GE GEnx-1B engine operators and producers,” the report acknowledged, suggesting that mechanical or programs failure just isn’t at the moment suspected.
The preliminary report factors towards human elements and cockpit administration as seemingly central points within the tragedy. The AAIB continues to research the gasoline cutoff occasion, the next engine relight makes an attempt, and the decision-making dynamics between the flight crew.


